SLA USES IN MOLDING FOR RAPID PROTOTYPING
Jim Mishek
Vista Technologies LLC
White
Bear Lake, MN
7 September 1997
IntroductionAs recent as three years ago the experts
were saying that injection molds made of stereolithograhy (SLA) produced
materials would never hold up. Fortunately, the machine owners did not listen to
the experts. We are no longer debating over if it will work. Instead the race
is, who can develop molds that produce a wide variety of part designs in a wide
variety of materials for the greatest number of shots in the shortest period of
time.
Wide variety of part designs, wide variety of materials, greatest number of
shots, shortest period of time, and we should add lowest in price. Because this
is a tough combination of parameters, these goals seem inherently paradoxical.
To make it easier to grasp, we have grouped these parameters into a three
dimension matrix, see figure 1. The Y-axis is for the variety of materials, the
X-axis is for the number of shots obtained, and the Z-axis is for the variety of
design criteria.

Figure 1
Before we go too far into the experimentation, it might be good to back up
and to examine why we are even interested in these processes.
BackgroundFit, Form, and Function are the three key
words defining the need for prototyping. With the advent of the various rapid
prototyping machines, particularly SLA, the need for Fit and Form has been
fulfilled. The problem is Function. In the proper application, we have succeeded
in building entire functioning models using the SLA material. But are the
properties the same as the materials to be used in the final product? NO.
Due to this dilemma came the advent of new technologies; the Selected Laser
Sintering (SLS) and the Fused Deposition Modeling (FDM). With both of these
technologies, you are able to assimilate the approximate properties of the
approximate materials that are to be used. These methods come closer, but they
still are not the real thing.
The search then reverted to trying to find some way to quickly manufacture
molds which could mold the real thing. The use of short run aluminum tooling was
examined, as well as the development of KelTool and the further development of
the SLS technology, enabling the manufacturing of metal tooling. Even in these
cases you are generally looking at a two to three week turn around and then you
still have to do additional machining which adds to the time.
The search continued. As mentioned earlier, despite the sage advise from the
experts, experimentation was carried out using solid blocks of the SLA material
as the injection molds themselves and it did work. This technique is referred to
as a solid ACES insert. ACES is an acronym for "Accurate Clear Epoxy Solid",
which is a build style for the SLA machines.
The major problems encountered with this technique were the amount of time it
took to make a solid mold, easily 30 hours, and the lack of heat transfer.1 The length of the build is height and volume
dependent.
The lack of heat transfer greatly reduces the variety of design parameters
and reduces the life of the mold faces due to the softness of the SLA material
at elevated temperatures above 60oC/140oF, and the material property changes at its glass
transition temperature of 70oC/158oF. At these elevated temperatures you can have mold
degradation through erosion or from spalling, where the mold material sticks to
the plastic and spalls off at ejection.2 Also, if
you can control the mold temperature more efficiently, you may be able to reduce
mold pressures which will increase mold life.3
The slow heat transfer, 300 times slower than tool steel, also means longer
cooling times for the parts before ejection. Periods of five minutes were not
unusual.
The next step was to go to a hollowed out SLA shell instead of a solid block,
these are called an ACES shell. In this method a mold shell is built on the SLA,
then copper tubing is inserted into the hollowed out area behind the mold face,
then the entire shell is filled with aluminum filled epoxy. This is the point
from which we began our experimentation to fill in the matrix.
ExperimentationExperiment 1: These trials involved
using a very simple shallow mold for a golf ball mark repair tool, seeing which
materials we could successfully run, and what tolerancing and longevity we could
get from the mold. The mold was made from an ACES shell with a face thickness of
1.5mm/.060" and side wall thickness of 2.5mm/.100", see figures 2 & 3.

Figure 2: The ACES shell mold
unfilled

Figure 3: The ACES mold
completed with molded parts
Experiment 2: The next tests were to study the design parameters. We
developed molds using low melting alloy as the fill material rather than epoxy,
then we combined this with molds that featured different design parameters such
as a thin, deep web, another tool that had very thin walls was designed into a
family mold, and a similar golf tool as in Experiment 1.
Experiment 1 was an interesting test, we did everything wrong and still got
good results. When completing the SLA mold shell, we allowed the shell to sit in
normal room conditions for two weeks before we tried to fill it. During this
time, the mold walls warped, approximately 3mm/.125", Requiring us to do extra
clean up before we could mount these shells into the mold base. Then, as we
tried to put the holes for the water lines in the shell wall by drilling, we
cracked the mold. This required us to glue the shell back together using the
same resin and a high intensity UV light.
The SLA material is very difficult to machine in the shelled condition
because of the vibrations. However, once the shell is filled the vibrations are
dampened, it is easy to machine. We performed milling, drilling, fly cutting,
and grinding with no complications.
The experimentation was run in a Cincinnati Milacron, 33 ton, Vista Sentry
injection molding machine, see Figures 4 & 5. In all of these tests the mold
was short shot to begin with and then adjusted accordingly until good parts were
produced. The shots took more pressure at the beginning until the mold warmed
up.
|
|
| Figure 4: The mold mounted into the
machine |
Figure 5: Measuring the temperature of the
mold face |
The table below shows the running parameters. The cooling was sufficient
enough to stabilize the temperature of the mold faces and to keep the
temperature of the mold faces below 57oC/135oF. With this style mold the cooling times were
approximately twice that of a steel mold. The polycarbonate required the highest
pressure, at one time reaching 15,390 psi, yet the mold held up. The proper
backing is very important, as you will see in the second experiment.
Experiment #1 Molding Results
| Material |
Avg. Press. |
Press Temp |
Water Temp |
Max Mold Temp |
Cycle Time |
# Pcs |
|
| Polypropylene |
5,280 psi |
220oC/425oF |
13oC/55oF |
48oC/120oF |
120 sec |
25 |
| ABS |
5,470 psi |
220oC/425oF |
13oC/55oF |
50oC/125oF |
100 sec |
25 |
| Cycoloy C2950, ABS/PC |
7,450 psi |
265oC/510oF |
43oC/110oF |
57oC/135oF |
80 sec |
14 |
| Polycarbonate |
11,110 psi |
293oC/560oF |
43oC/110oF |
57oC/135oF |
100 sec |
10 |
| Nylon 8018, 14% glass |
7,530 psi |
293oC/560oF |
43oC/110oF |
54oC/130oF |
100 sec |
3 |
As we ran each test, we numbered each part. Later each part was measured and
inspected, see Figures 6 & 7. The chart below shows the results.
Experiment #1 Dimensional Stability of Parts
| Material |
Avg Meas A |
Avg Meas B |
Avg Meas C |
Avg Meas D |
|
| Polypropylene |
.698 +/- .001 |
.180 +/- .001 |
.238 +/- .002 |
.241 +/- .001 |
| ABS |
.709 +/- .001 |
.189 +/- .001 |
.254 +/- .001 |
.251 +/- .001 |
| Cycoloy C2950, ABS/PC |
.705 +/- .001 |
.185 +/- .001 |
.249 +/- .002 |
.246 +/- .002 |
| Polycarbonate |
.705 +/- .001 |
.184 +/- .003 |
.248 +/- .003 |
.246 +/- .002 |
| Nylon 8018, 14% glass |
.703 +/- .001 |
.178 +/- .001 |
.236 +/- .003 |
.239 +/- .003 |
As you can see, the dimensional stability is quite good. When examining the
parts, you will see that the mold had started to erode. This happened when we
started to shoot the polycarbonate. Whether this is just from the conditions of
molding polycarbonate or if it was a cumulative effect of the previous shots, we
can not conclude at this time.
The eventual mode of failure was twofold. There was the erosion of the faces
and there was a blow out through the edge of the mold near the tips of the tines
of the tool.
The second cause of failure points out that good mold design is still a must.
This is proven in the second experiment as well. This mold should have had two
small ejectors near the tips of the tines to aid in the ejection as well as to
serve as vents. The mold face shows the effect of the hot gases being forced
into the tines and then having to find its way out - eventually the thin wall
gave way. On the mold faces you are able to see the traces of the gases escaping
through the parting lines.
|
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| Figure 7: This diagram shows the location of
the measurements. |
Figure 8: The parts were identified for future
inspection. Notice the flashing near the tines on the last parts molded.
|
The conclusion from these tests is: the ACES shell mold will accept a wide
variety of materials with some higher heats and pressures and will produce good
parts, the quantity appears to vary dependant on the material, more
experimentation for life expectancy needs to be done for each material.
We decided that before we chased down this path, we wanted to try to perfect
the mold design aspects first. We believe if we can cool the part quicker, we
can obtain longer life (due to the less time that the mold faces spend in their
vulnerable temperature range).
Therefore, Experiment 2 concentrated on trying to get the low melting metal
to work as a backing material. The low melting metal (lmm) is a mixture of lead
and bismuth. Depending on the alloying percentages, you can have an alloy which
melts between 50oC/120oF and in excess of 100oC/210oF.
The lmm was much tougher to work with than the epoxy. If we were not careful
we could overheat the lmm and then when we tried to pour the lmm into the mold
face, the face warped and we lost dimensional integrity. We did successfully
mount the faces into the mold bases, see figures 8 & 9.
Unfortunately, we never had any totally successful shots using this
technique. We had mold face spalling and we had mold face deformation. See
figure 10. The fascinating problem with the lmm is that it does not bond to the
SLA material which makes up the mold face. When the face tried to move due to
thermal forces, there was nothing there to hold it. The mold with the deep web
failed when the face of the web pocket distorted and froze the part into the
mold. The lmm also proved not to be an adequate backing material. Our mold faces
were pushed back .5mm/.020", which ruined our shut offs and created excessive
flashing.
|
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| Figure 8: This is the face of the watch mold.
|
Figure 9: The cavity of the golf repair tool
mounted into the mold base. |
There were minor successes in these failures. The detail we managed to
achieve in the thin wall sections was excellent and it proved once again how
important mold design and mold preparation is for success. The one thin watch
part would have been successful except for the lack of venting, gas built up in
the center of the part. This same part began to show erosion in one of the cored
areas because enough care was not taken in the mold preparation. This area still
had stair stepping, so when the parts were ejected they eroded the mold face.
See Figures 11-13.
We did achieve our goal of fast cooling. The low melting metal did allow us
to run parts at similar speeds to metal molds, while keeping the mold face
temperatures at near our cooling water temperature.
ConclusionThe ACES shell design is an adequate
design for producing parts for a wide variety of materials. Future testing
should be done using the aluminum filled epoxy rather than the low melting
metal. However, the goal should still be to get the heat away from the SLA mold
faces quicker. Additional work should be pursued on coatings as well. The most
recent tests published have shown good results with nickel coatings when running
ABS, but minuscule gains when running polycarbonate.
4
A final note that keeps reappearing in all of our tests, mold design is of a
premium. The fact that you can not run 50 parts to fine tune your mold with a
SLA mold, requires the mold designer to over design the mold for vents and
ejection. It is also important to develop a range of operating parameters so the
press operator can produce successful parts quickly.
|
|
| Figure 10: Notice the deformation in the center
of the part due to a break out, also notice the pieces of spall on the thumb
indent and by the gate. |
Figure 11: These parts had thin webs, over an
inch in depth. |
|
|
| Figure 12: Note the thin wall sections and the
fine detail. This came from a family mold. |
Figure 13: the molded watch case and the original
SLA prototypes. |
AcknowledgmentsVista Technologies wishes to thank
Imperial Custom Mold for their design efforts, molding expertise, and press
availability. We, also wish to thank Spectrum Mold for their expert mold design
and molding expertise along with Donnelly Custom Manufacturing for their molding
expertise and machine availability.
References1. Jacobs, Paul, 1996, Recent
Advances in Rapid Tooling From Stereolithography, 3D Systems, pp. 4-7.
2.
Decelles, Paul, 1996, Direct AIM Prototype Tooling Procedure Guide, 3D Systems,
p. 9.
3. Dell’Arciprete, John, 1997, Cavity Pressure Studies for
Stereolithography Produced Tooling, IPI, University of Massachusetts Lowell, p.
1.
4. Burns, David T., 1997, Analysis of Metal Coating Effects on
Stereolithography Tooling for Injection Molding, IPI, University of
Massachusetts Lowell, pp. 1, 10-12.